The operator of a 280 kWp rooftop system on a cold storage facility in Schleswig-Holstein (20 km from the North Sea coast) noticed a gradual yield decline from the 4th year of operation. The monitoring data revealed a conspicuous pattern: strings with negative grounding polarity (minus pole grounded at the inverter) lost disproportionate power, while positive strings were barely affected.
| String group | Strings | Pmax (STC, nominal) | Pmax (STC, actual) | Deviation |
|---|---|---|---|---|
| Positive polarity (inverter+ grounded) | 8 | 140 kWp | 131.6 kWp | −6.0% (age-related) |
| Negative polarity (inverter− grounded) | 8 | 140 kWp | 96.6 kWp | −31.0% |
The 25 percentage point difference between the positive and negative side is the classic PID indicator.
The EL images of the modules at the negative string end showed the PID-typical pattern: edge cells (particularly the outer 2–3 cell rows) were partially to fully inactive (dark in EL). The degree of inactivation decreased with increasing distance from the grounding point — a clear PID profile.
The shunt resistances (Rsh) of the affected modules ranged from 8–45 ohm. Unaffected modules showed Rsh values of 200–800 ohm. The low shunt resistance confirms the leakage-current-induced degradation mechanism (Na+ ion migration in the anti-reflective coating).
In November 2024, a PID regeneration attempt was conducted: application of positive voltage (+1,000 V DC, module frame against cells) during nighttime hours over 21 days. Result:
| Time point | Pmax neg. strings | Regeneration |
|---|---|---|
| Before regeneration (Sep 2024) | 96.6 kWp (−31%) | — |
| After 7 days | 108.2 kWp (−22.7%) | +8.3 pp |
| After 14 days | 114.8 kWp (−18.0%) | +13.0 pp |
| After 21 days (completion) | 121.8 kWp (−13.0%) | +18.0 pp |
The regeneration plateaued after 21 days — the remaining 13% loss is to be considered irreversible (permanently damaged cell structures).
| Item | Amount |
|---|---|
| Cumulative yield loss (years 4–6, progressive PID) | EUR 52,800 |
| Irreversible permanent damage (−13% on 140 kWp, NPV 15 years) | EUR 68,400 |
| PID regeneration system (retrofit anti-PID box) | EUR 4,200 |
| Assessment + EL + IV measurement | EUR 12,600 |
| Total damage | EUR 138,000 |
The module manufacturer's performance warranty (90% after 10 years, 80% after 25 years) is clearly breached at −31% after 6 years. A warranty claim for module replacement is justified.
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Request a consultationLast updated: 2026-06-16 | Author: Christoph S. Prestele, TUV-certified expert assessor | PV-BESS-Assessor.com